Whiting Gets The Peery State (#16463) Back Into Production -- March 30, 2018

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Title : Whiting Gets The Peery State (#16463) Back Into Production -- March 30, 2018
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Whiting Gets The Peery State (#16463) Back Into Production -- March 30, 2018

The well:
  • 16463, 1,081, Whiting, Peery State 11-25H, Sanish, t5/0; 385K as of 9/15; now 397K 1/8; very little production after 2014; ... until mid-2017
I had not updated this well since September, 2015. That's about 2.5 years ago. I've gone through all the 16XXX wells, the 17XXX wells, the 18XXX wells, and am working through the 19XXX wells -- and there are thousands of Bakken wells drilled between 2007 and 2011 that are "lousy" wells.

So, going through all these thousands of wells, here's what can happen in the Bakken, something we don't see in conventional plays.

In October, 2013, for all practical purposes this well was taken off-line; occasionally there was some production.

Here's an example of the production in CY 2014:
BAKKEN 12-2014 1 3 3 1 21 19 0
BAKKEN 11-2014 4 2 3 2 8 0 0
BAKKEN 10-2014 31 78 86 42 66 4 0
BAKKEN 9-2014 30 713 711 142 450 260 131
BAKKEN 8-2014 4 258 251 55 237 129 101
BAKKEN 7-2014 0 0 0 0 0 0 0
BAKKEN 6-2014 0 0 0 0 0 0 0
BAKKEN 5-2014 0 0 0 0 0 0 0
BAKKEN 4-2014 0 0 0 0 0 0 0
BAKKEN 3-2014 0 0 0 0 0 0 0
BAKKEN 2-2014 0 0 0 0 0 0 0
BAKKEN 1-2014 0 0 0 0 0 0 0

Here's an example of the production from this well in CY 2016:
BAKKEN 12-2016 0 0 1 0 0 0 0
BAKKEN 11-2016 3 10 9 47 4 0 0
BAKKEN 10-2016 0 0 0 0 0 0 0
BAKKEN 9-2016 0 0 0 0 0 0 0
BAKKEN 8-2016 0 0 0 0 0 0 0
BAKKEN 7-2016 0 0 0 0 0 0 0
BAKKEN 6-2016 0 0 0 0 0 0 0
BAKKEN 5-2016 0 0 0 0 0 0 0
BAKKEN 4-2016 1 4 4 20 2 0 0
BAKKEN 3-2016 1 1 1 8 2 0 0
BAKKEN 2-2016 1 0 0 17 2 0 0
BAKKEN 1-2016 1 1 1 9 2 0 0

Maybe someone smarter than I can see the incredible difference in production between 2015 and 2016. I can't.

But prior to 2014, it was a pretty good well:
BAKKEN 9-2013 25 1143 1246 55 2242 2094 100
BAKKEN 8-2013 31 2466 2391 171 2782 2649 71
BAKKEN 7-2013 31 2576 2692 277 2980 2918 0
BAKKEN 6-2013 25 2830 2838 346 2053 2007 0
BAKKEN 5-2013 31 3480 3350 231 3353 3291 0
BAKKEN 4-2013 30 3637 3703 182 3418 3358 0

So, pretty much a dead well after 2015? Apparently not.

Look at the production starting in June, 2017:
Pool Date Days BBLS Oil Runs BBLS Water MCF Prod MCF Sold Vent/Flare
BAKKEN 1-2018 31 1502 1665 619 2127 2065 0
BAKKEN 12-2017 31 1504 1342 846 2747 2685 0
BAKKEN 11-2017 30 1440 1430 1048 2712 2652 0
BAKKEN 10-2017 31 1464 1461 1137 2745 2683 0
BAKKEN 9-2017 30 1473 1481 1681 2511 2451 0
BAKKEN 8-2017 31 1759 1786 1374 2159 2097 0
BAKKEN 7-2017 31 1626 1594 1354 1659 1597 0
BAKKEN 6-2017 27 1080 1066 2539 1162 1108 0

So, what happened?

FracFocus: no evidence that this well has been re-fracked. No evidence that this has anything to do with neighboring wells.

But, then there's a sundry formed received by the NDIC, June 2, 2017, for work completed May 23 2017: "Due to a tight spot found at ~8,180' in the HCL-80 casing, Whiting Petroleum set a 5.5" permanent packer at 8700' with 2500' of 5.5", 23 ppf scab liner above it with liner top packer."

An attached19-page diagram suggests work was begun April 11, 2017. The total AFE was $950,000. With the work-over, how is the well doing?

Pool Date Days BBLS Oil Runs BBLS Water MCF Prod MCF Sold Vent/Flare
BAKKEN 1-2018 31 1502 1665 619 2127 2065 0
BAKKEN 12-2017 31 1504 1342 846 2747 2685 0
BAKKEN 11-2017 30 1440 1430 1048 2712 2652 0
BAKKEN 10-2017 31 1464 1461 1137 2745 2683 0
BAKKEN 9-2017 30 1473 1481 1681 2511 2451 0
BAKKEN 8-2017 31 1759 1786 1374 2159 2097 0
BAKKEN 7-2017 31 1626 1594 1354 1659 1597 0
BAKKEN 6-2017 27 1080 1066 2539 1162 1108 0
BAKKEN 5-2017 0 0 0 0 0 0 0
BAKKEN 4-2017 0 0 0 0 0 0 0


This well, #16463, was a tri-lateral horizontal. See graphic below. None of the neighboring wells were taken off-line while this well was being re-worked.









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