Idle Rambling -- #16952 -- MRO's Christensen 34-33H In Bailey Field

Idle Rambling -- #16952 -- MRO's Christensen 34-33H In Bailey Field - Hallo friendsMY LIVE MY WAY, In the article you read this time with the title Idle Rambling -- #16952 -- MRO's Christensen 34-33H In Bailey Field, We have prepared this article for you to read and retrieve information therein. Hopefully the contents of postings Article my style, Article my way, Article New ways, Article their way, We write this you can understand. Alright, good read.

Title : Idle Rambling -- #16952 -- MRO's Christensen 34-33H In Bailey Field
link : Idle Rambling -- #16952 -- MRO's Christensen 34-33H In Bailey Field

Read too


Idle Rambling -- #16952 -- MRO's Christensen 34-33H In Bailey Field

I noted this last summer, August, 2017, I suppose:
  • 16952, MRO, a nice well; candidate for re-frack; off-line these last two months (9/17);
So, let's see what came of this well. LOL.

First, the production profile since then:
Pool Date Days BBLS Oil Runs BBLS Water MCF Prod MCF Sold Vent/Flare
BAKKEN 5-2018 31 14514 14363 11435 8077 982 5988
BAKKEN 4-2018 30 17304 17336 13971 9922 19 7876
BAKKEN 3-2018 25 19238 19124 15911 11003 31 8771
BAKKEN 2-2018 21 11675 11788 9983 7031 183 5488
BAKKEN 1-2018 31 24507 24442 23245 14326 4930 6591
BAKKEN 12-2017 17 15876 16004 13712 10632 3632 5214
BAKKEN 11-2017 24 13304 13104 11367 8961 0 7399
BAKKEN 10-2017 28 24230 24268 10559 16308 0 13557
BAKKEN 9-2017 0 0 0 0 0 0 0
BAKKEN 8-2017 0 0 0 0 0 0 0
BAKKEN 7-2017 0 0 0 0 0 0 0
BAKKEN 6-2017 1 27 0 220 13 0 10
BAKKEN 5-2017 30 654 649 202 488 35 205
BAKKEN 4-2017 30 762 742 209 567 296 11
BAKKEN 3-2017 31 803 808 220 604 306 28
BAKKEN 2-2017 28 680 697 194 513 256 16

It's an MRO well in Bailey oil field, so the odds are that it was a re-fracked well. Let's check FracFocus, API - 33-025-00699: yup, re-fracked, 9/18/17- 9/30/17. From FracFocus: 4.1 million gallons water (moderate re-frack); 85.7% water.
  • 16952, 508, MRO, Christensen 34-33H, Bailey, t6/08; cum 332K 5/18
From the operator's sundry form:
  • new IP: 1,550
  • test: 10/8/2017
  • middle Bakken
  • 45 stages
  • 5.5 million lbs (a medium frack)
  • 123K pounds/stage (less than the usual 200,000 lbs/stage)
Neighboring wells:
  • 22658, taken off-line during the re-rack but no jump in production;
  • 18681, not taken off-line for this frack, but a very, very nice well; jump in production back in 12/14; perhaps I will check up on that later;
  • 18842, another huge jump in production, but it was obviously re-fracked; maybe I will check up on it later;
The MRO roughnecks are monsters -- slamming the Bailey with these re-fracks.






Thus Article Idle Rambling -- #16952 -- MRO's Christensen 34-33H In Bailey Field

That's an article Idle Rambling -- #16952 -- MRO's Christensen 34-33H In Bailey Field This time, hopefully can give benefits to all of you. well, see you in posting other articles.

You are now reading the article Idle Rambling -- #16952 -- MRO's Christensen 34-33H In Bailey Field with the link address https://mylivemyidea.blogspot.com/2018/07/idle-rambling-16952-mros-christensen-34.html

Subscribe to receive free email updates:

Related Posts :

0 Response to "Idle Rambling -- #16952 -- MRO's Christensen 34-33H In Bailey Field"

Post a Comment