Incredible Story: CLR's Whitman Wells in Oakdale Oil Field -- July 31, 2018

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Title : Incredible Story: CLR's Whitman Wells in Oakdale Oil Field -- July 31, 2018
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Incredible Story: CLR's Whitman Wells in Oakdale Oil Field -- July 31, 2018

I originally posted this note over the weekend. A major error was noted by a reader. I found the entire "story" so interesting that I have moved the entire post here.

Hopefully, no errors of substance this time.

This is an incredibly interesting story on so many levels, but  a huge shout out to the roughnecks and the safety team for a successful re-entry in a very dicey operation. This story speaks volumes about the skills, professionalism, can-do attitude of the entire team involved in this operation, and probably indicative of most operations in the Bakken. So without further ado, the new post.

Updates

July 31, 2018: huge mistake on my part regarding the Whitman wells. See comment from reader at the original post. Corrections and clarifications have been made -- continue reading.

First correction is easy:
  • 20210, 803, CLR, Whitman 2-34H, Oakdale, API - 33-025-01259; t9/11; cum 1.595 million bbls 5/18; see production profile below; FracFocus: no re-frack; original frack, 24 stages; 2.4 million lbs sand; in addition to the 1.6 million bbls of oil, a cum of 1650315 MCF gas (275K boe natural gas -- so we're talking close to 2 million boe so far;
Second correction (not a correction so much as an update): as the reader noted, the original #20212 was not drilled to planned depth and not completed back in 2011 due to downhole issues. Last summer, CLR went back in, drilled to planned depth and fracked the well. From the file report:
  • spud date: January 19, 2011
  • original TD date: April 23, 2011 -- to 13,681 feet, equivalent to a short lateral
  • re-entry date: July 5, 2017
  • TD date: July 8, 2017 (only three days to drill to depth after re-entry)
  • TD: 21,230 feet
  • an Upper Devonian Three Forks well within the Rocket prospect
  • introduction: Well drilling operations ceased on April 23, 2011, after dangerous levels of oil and gas pressure rendered further drilling unwise at the time. The well has been in production in its incomplete form (13681' MD reached, open hole, no fracking) since that time and has produced approximately 120,000 bbls of petroleum.  
  • this report primarily concerns re-entry drilling information only, as complete data from the original drilling was generated by a different mud-logging company and is at points incomplete. Where available, salient points from the original drilling events have been included.
  • the well plan ... three scenarios were foreseen ... the rig operators prepared for all events, the high-pressure scenario being the most dangerous, but likely manageable...
  • original (back in 2011) drilling efforts ceased at 13681' MD for high (dangerous) levels of oil and gas pressures. As of 2017, these were deemed low enough for re-entry to attempt drilling to the originally planned TD point, hopefully to produce at least moderate amounts of oil, as indicated by original production levels.
  • background gas levels were initially 600 - 1200 units with circulation through the gas buster, which was activated after the first trip gas at 10,000 units. This well had been hard to control when the first segment was drilled in 2011, so all precautions for safety and control were observed.  
  • gas increased to 1800 - 2200 units at 17500' MD, when the formation took a relatively sharp turn and then rolled over, similar to the structure observed from the initial segment and may have signaled a fracture and/or stratigraphic trap of less, but still significant, production as the first one.
  • the Upper Devonian Three Forks formation was intercepted at 11596' TVD ( ~ 8618' SS).
  • it was determined initially that the ideal target would be approximately 15' thick, beginning 15' below the Three Forks top, and extending to 30' below the same reference point.
Original Post 

Is Something Going On With CLR's Whitman Wells?
Yup: A Re-Entry And Frack Of A Well That Was "Aborted" Back In 2011 Due To Dangerous Gas Levels

Section 34-147-96, Oakdale oil field; only three older wells sited in this section. One was off-line for a few months recently and is now back on line; the other two are now off line. FrackFocus will be checked.

The wells:
  • 17061, 664, CLR, Whitman 11-34H, Oakdale, API - 33-025-00723; t6/08; cum 446K 5/18; see production profile below; FracFocus: no re-frack;
  • 20210, 803, CLR, Whitman 2-34H, Oakdale, API - 33-025-01259; t9/11; cum 1.595 million bbls 5/18; see production profile below; FracFocus: no re-frack; original frack, 24 stages; 2.4 million lbs sand; in addition to the 1.6 million bbls of oil, a cum of 1650315 MCF gas (275K boe natural gas -- so we're talking close to 2 million boe so far;
  • 20212, 482, CLR, Whitman 3-34H, Oakdale, API - 33-025-01261; t9/11; cum 181K 5/18; see production profile below; well, isn't this interesting -- yup, this well was fracked 9/23/17 - 10/5/17; 9.8 million gallons of water; 84% water; 15% sand; sundry form in file report: 61 stages; 14.5 million lbs sand; 
The graphic:


17061:
Pool Date Days BBLS Oil Runs BBLS Water MCF Prod MCF Sold Vent/Flare
BAKKEN 5-2018 31 2378 2220 154 2695 2394 54
BAKKEN 4-2018 30 2371 2166 160 2724 2484 0
BAKKEN 3-2018 31 2440 2387 152 2619 2342 30
BAKKEN 2-2018 28 2294 2581 111 2251 2027 0
BAKKEN 1-2018 6 496 0 40 351 303 0
BAKKEN 12-2017 1 0 0 0 11 11 0
BAKKEN 11-2017 2 0 0 0 22 22 0
BAKKEN 10-2017 0 0 0 0 0 0 0
BAKKEN 9-2017 7 420 545 30 669 613 0
BAKKEN 8-2017 31 1972 2157 114 3054 2806 0
BAKKEN 7-2017 31 1982 1811 115 2914 2448 218

20210 (a huge, huge well):
Pool Date Days BBLS Oil Runs BBLS Water MCF Prod MCF Sold Vent/Flare
BAKKEN 5-2018 0 0 0 0 0 0 0
BAKKEN 4-2018 0 0 0 0 0 0 0
BAKKEN 3-2018 0 0 221 0 0 0 0
BAKKEN 2-2018 0 0 0 0 0 0 0
BAKKEN 1-2018 0 0 0 0 0 0 0
BAKKEN 12-2017 2 0 0 19 0 0 0
BAKKEN 11-2017 3 22 0 21 1 0 0
BAKKEN 10-2017 3 2 38 0 1 0 0
BAKKEN 9-2017 16 3829 3858 232 4800 4703 0
BAKKEN 8-2017 31 9112 9143 428 10829 10590 0
BAKKEN 7-2017 26 6257 6352 117 6851 5326 1380
BAKKEN 6-2017 30 9377 9406 333 11517 11284 0
BAKKEN 5-2017 31 10218 10106 357 12107 11861 0
BAKKEN 4-2017 28 8004 8101 327 9332 8923 220
BAKKEN 3-2017 31 10149 10137 318 11626 11381 0
BAKKEN 2-2017 28 9545 9446 285 10713 10494 0
BAKKEN 1-2017 31 10635 10757 350 12042 11508 297
BAKKEN 12-2016 31 10697 10584 315 11582 11354 0
BAKKEN 11-2016 29 10539 10689 355 11311 11096 0
BAKKEN 10-2016 31 11462 11484 315 12258 12010 0
BAKKEN 9-2016 19 8745 8486 137 8366 8217 0
BAKKEN 8-2016 0 0 237 0 0 0 0
BAKKEN 7-2016 30 10534 10558 350 11332 10035 1065
BAKKEN 6-2016 30 11354 11279 440 12596 8945 3412
BAKKEN 5-2016 31 12067 11991 479 14115 13656 212
BAKKEN 4-2016 27 10189 10128 528 11146 10973 0

20212:
Pool Date Days BBLS Oil Runs BBLS Water MCF Prod MCF Sold Vent/Flare
BAKKEN 5-2018 0 0 403 0 0 0 0
BAKKEN 4-2018 16 3239 3127 473 2465 2376 0
BAKKEN 3-2018 19 5486 5631 756 4317 4139 50
BAKKEN 2-2018 25 5310 5088 595 4445 4261 0
BAKKEN 1-2018 31 10513 10725 1869 8937 8641 50
BAKKEN 12-2017 31 21903 21790 4841 24087 23839 0
BAKKEN 11-2017 30 19452 19809 5379 19667 18479 968
BAKKEN 10-2017 21 12150 11401 6847 13549 7191 6268
BAKKEN 9-2017 0 0 0 0 0 0 0
BAKKEN 8-2017 0 0 0 0 0 0 0
BAKKEN 7-2017 0 0 0 0 0 0 0
BAKKEN 6-2017 0 0 0 0 0 0 0
BAKKEN 5-2017 1 0 0 2 0 0 0
BAKKEN 4-2017 5 380 363 98 115 114 0
BAKKEN 3-2017 6 157 320 0 108 99 0
BAKKEN 2-2017 4 162 170 0 174 0 158
BAKKEN 1-2017 3 158 284 0 154 0 153
BAKKEN 12-2016 2 147 0 0 162 0 146
BAKKEN 11-2016 3 152 184 0 5 0 0
BAKKEN 10-2016 2 151 278 2 123 115 0
BAKKEN 9-2016 3 148 0 0 3 0 0
BAKKEN 8-2016 2 141 0 2 80 0 80
BAKKEN 7-2016 7 189 203 25 89 88 0


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